air leak in the manifold would be my guess. Remove the manifold and fit a
new gasket and also check the carb seals/gaskets whilst at it as its easy to
replace them while the carbs are off.
"whawes" <wdhawes.RemoveThis@gmail.com> wrote in message
news:1166391537.440450.232310@79g2000cws.googlegroups.com...
I've recently purchased a 1972 1275 GT, which runs pretty well but has
the following problems:
1) When I first got the car it would stall immediately at normal
operating temperature unless run with the choke approx 3/4 inch out. I
took it to a local garage who told me it was running too lean, so they
richened it up and reset the idle speed. They (MG specialists so
presumably familiar with Mini engines) thought it might have an
aftermarket cam fitted as the engine pulls very strongly at higher rpm.
I've now wired up the rev counter, which shows the car sometimes idles
OK at 750rpm with the choke fully in, but more often than not will
stall unless idle speed is raised to about 1000rpm, particularly when
coming to a standstill at junctions. Would an aftermarket cam alone
explain the above? 1000rpm seems a bit high to me.
2) The car misfires/exhaust pops noticeably above 4000rpm. Below
4000rpm it seems OK, there is a slight chug from the exhaust at idle
and an occasional pop on the overrun. The exhaust is the straight
through, large bore type with twin centre exit. I've got a 998cc Mini
with the same exhaust which doesn't pop on the overrun so I'm guessing
this isn't normal.
3) There is a strong smell of fuel in the cabin after approx 5 minutes
of running. It seems to be coming from the carb and gets noticeably
stronger after hard acceleration. I've had the car idling with the
bonnet up and can't see any evidence of a fuel/vacuum leak.
4) Fuel consumption seems a bit high. I put nearly a full tank of fuel
in on Friday evening (£15) and have done approx 60 miles of mixed
driving since. The gauge now reads 1/4 full, which I make just over 30
mpg. Maybe I'm optimistic but I was expecting closer to 40mpg - my Mini
1000 will do well over 40mpg under normal use. The exhaust tailpipes
are quite sooty, if the mixture had not been checked so recently I'd
wonder if it was set too rich.
5) The throttle has stuck part way open a couple of times (dabbing the
accelerator once or twice unsticks it). Is this down to a sticking
needle in the carb?
In the fault finding section of my Haynes manual, problems (1), (2) and
(3) have a flooded float chamber on the carb / incorrect float height
listed as being a possible cause.
I'm thinking about removing the carb and servicing it. Sound like a
good idea? All suggestions appreciated.
TIA
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